The Kegworth air disaster occurred on 8 January 1989 when British Midland Flight 92, a Boeing 737-400, crashed onto the embankment of the M1 motorway near Kegworth, Leicestershire, UK. The aircraft was attempting to conduct an emergency landing at East Midlands Airport. Of the 126 people aboard, 47 died and 74, including seven members of the flight crew, sustained serious injuries.
History
The aircraft was a British Midland operated Boeing 737-400, registration G-OBME, on a scheduled flight from London Heathrow Airport to Belfast International Airport, Northern Ireland, having already flown from Heathrow to Belfast and back that day.
Incident
After taking off from Heathrow at 7:52 pm, Flight BD 092 was climbing
through 28,300 feet to reach its cruising altitude of 35,000 feet when a
blade detached from the fan of the port (left) engine. While the pilots
did not know the source of the problem, a pounding noise was suddenly
heard, accompanied by severe vibrations.
In addition, smoke poured into the cabin through the ventilation system
and a burning smell entered the plane. Several passengers sitting near
the rear of the plane noticed smoke and sparks coming from the left
engine. The flight was diverted to nearby East Midlands Airport at the suggestion of British Midland Airways Operations.
After the initial blade fracture, Captain Kevin Hunt had disengaged the plane's autopilot. When Hunt asked First Officer
David McClelland which engine was malfunctioning, McClelland replied:
"It's the le... No, the right one". In previous versions of the 737, the
left air conditioning pack, fed with compressor bleed air from the left
(number 1) engine, supplied air to the flight deck, while the right air
conditioning pack, fed from the right (number 2) engine supplied air to
the cabin. On the 737-400 this division of air is blurred; the left
pack feeds the flight deck but also feeds the aft cabin zone, while the
right feeds the forward cabin. The pilots had been used to the older
version of the aircraft and did not realise that this aircraft (which
had only been flown by British Midland for 520 hours over a two-month
period) was different. The smoke in the cabin led them to assume the
fault was in the right engine. The pilots throttled back the working
right engine instead of the malfunctioning left engine. They had no way
of visually checking the engines from the cockpit, and the cabin
crew—who did not hear the commander refer to the right hand engine in
his cabin address—did not inform them that smoke and flames had been
seen from the left engine.
When the pilots completely shut down the right engine, they could no
longer smell the smoke, which led them to believe that they had
correctly dealt with the problem. As it turned out, this was a
coincidence: when the autothrottle
was disengaged to shut down the right engine, the fuel flow to the left
engine was reduced, and the excess fuel which had been igniting in the
jet exhaust disappeared; therefore, the ongoing damage was reduced, the
smoke smell ceased, and the vibration reduced, although it would still
have been visible on cockpit instruments.
During the final approach to the East Midlands Airport,
more fuel was pumped into the damaged engine to maintain speed, which
caused it to cease operating entirely and burst into flames. The flight
crew attempted to restart the right engine by windmilling,
using the air flowing through the engine to rotate the turbine blades
and start the engine, but the aircraft was by now flying at 185 km/h,
too slow for this. Just before crossing the M1 motorway,
the tail struck the ground and the aircraft bounced back into the air
and over the motorway, knocking down trees and a lamp post before
crashing on the far embankment and breaking into three sections
approximately 519yd (1/4-mile or 475 metres) short from the active runway's
paved surface and approximately 689yd (1/3-mile or 630 metres) from its
threshold. Remarkably, there were no vehicles on that part of the
motorway at the moment of the crash.
Casualties
Of the 118 passengers on board, 39 were killed outright in the crash and
eight were fatally injured and died later, for a total of 47
fatalities. All eight members of the crew survived the accident. Of the
79 survivors, 74 suffered serious injuries and five suffered minor
injuries.
No one on the motorway was injured, and all vehicles in the vicinity of
the disaster were undamaged. The first person to arrive at the scene to
render aid was a motorist—a former Royal Marine who helped passengers
for over three hours—who subsequently received damages for post-traumatic stress disorder.
Causes
Shutting down the wrong engine
The Captain,
Kevin Hunt, believed the right engine was malfunctioning due to the
smell of smoke in the cabin because in previous Boeing 737 variants bleed air
for cabin air conditioning was taken from the right engine and also
because the right engine fire warning light was flashing. However,
starting with the Boeing 737-400 variant, Boeing redesigned the system
to use bleed air from both engines. Several cabin staff and passengers
noticed that the left engine had a stream of unburnt fuel igniting in
the jet exhaust, but this information was not passed to the pilots
because cabin staff assumed the pilots were aware that the left engine
was malfunctioning.
The smell of smoke disappeared when the autothrottle was disengaged
and the right engine shut down due to reduction of fuel to the damaged
left engine as it reverted to manual throttle. In the event of a
malfunction pilots are trained to check all meters and review all
decisions, and Captain Kevin Hunt proceeded to do so. Whilst he was
conducting the review, he was interrupted by a transmission from East
Midlands Airport informing him he could descend further to 12,000 feet
(3,700 m) in preparation for the diverted landing. He did not resume the
review after the transmission ended, and instead commenced descent. The
vibration indicators were smaller than on the previous versions of the
737 in which the pilots had the majority of their experience.
The dials on the two vibration gauges (one for each engine) were
small and the LED needle went around the outside of the dial as opposed
to the inside of the dial as in the previous 737 series aircraft. The
pilots had received no simulator training on the new model as no
simulator for the 737-400 existed in the UK at that time. At the time
vibration indicators were known for being unreliable
(and normally ignored by pilots) but unknown to the pilots this was one
of the first aircraft to have a very accurate vibration readout.
Engine malfunction
Analysis of the engine from the crash determined that the fan blades (LP Stage 1 compressor) of the uprated CFM56
engine used on the 737-400 were subject to abnormal amounts of
vibration when operating at high power settings above 25,000 feet
(7,600 m). As it was an upgrade to an existing engine, in-flight testing
was not mandatory, and the engine had only been tested in the
laboratory. Upon this discovery all 99 Boeing 737-400s
(since G-OBME had crashed) were grounded and the engines modified.
Following the crash, it is now mandatory to test all newly designed and
significantly redesigned turbofan engines under representative flight conditions.
This unnoticed vibration created excessive metal fatigue
in the fan blades, and on G-OBME this caused one of the fan blades to
break off. This damaged the engine terminally and also upset its
delicate balance, causing a reduction in power and an increase in
vibration. The autothrottle attempted to compensate for this by
increasing the fuel flow to the engine. The damaged engine was unable to
burn all the additional fuel, with much of it igniting in the exhaust
flow, creating a large trail of flame behind the engine.
Aftermath
The official report into the disaster made 31 safety recommendations.
Evaluation of the injuries sustained led to considerable improvements
in aircraft safety and emergency instructions for passengers. These
were derived from a research programme funded by the CAA and carried out
by teams from the University of Nottingham
and Hawtal Whiting Structures (a consultancy company). The study
between medical staff and engineers used analytical "occupant
kinematics" techniques to assess the effectiveness of the brace position. A new notice to operators revising the brace position was issued in October 1993.
There is a memorial to "those who died, those who were injured and
those who took part in the rescue operation", in the village cemetery in
nearby Kegworth, together with a garden made using soil from the crash site.
Captain Kevin Hunt and First Officer David McClelland |
Alan Webb, the Chief Fire Officer at East Midlands Airport, was awarded an MBE in the 1990 New Year Honours list for the co-ordination of his team in the rescue efforts that followed the crash.
Graham Pearson, a man who assisted Kegworth survivors, sued the airline and was awarded £57,000 in damages in 1998.
Source:
http://en.wikipedia.org/wiki/Kegworth_air_disaster
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